some weird things are happening with my boards (custom made)
- I tried to program initially with TWR example from github https://github.com/Decawave/dwm1001-examples . I programmed successfully then later I am not able to access my controller. Error: Target not found.
- Why the GPIO’s are configured differently in the TWR_initiator code DWM1001_Dev.h. I can see RESET pin is configured to pin 24. Actually it is pin no 33. Am I right?
It is strange that everything works perfect with DWM1001-DEV.
3.After programming TWR Initiator code, my board is continuously getting restarted. I doubt that is because
/* Reset DW1000 */
Any idea what is happening.